Status Update 12/7

This week we integrated our two codebases so the project has all the needed functionality.  We also began working on the panel and photoresitor mounting to the servo motor.  Unfortunately a wiring mistake led to us burning up out PowerBoost, meaning we are no longer able to run the project off the battery.  There was not enough time to order a new unit, so we instead are running the servo off of a 5V supply and are using another variable supply as an analogue for the battery.  While not ideal, this allows us to showcase all the functionality the code has to offer.

Leave a Reply

Your email address will not be published. Required fields are marked *