This week we integrated our two codebases so the project has all the needed functionality. We also began working on the panel and photoresitor mounting to the servo motor. Unfortunately a wiring mistake led to us burning up out PowerBoost, meaning we are no longer able to run the project off the battery. There was not enough time to order a new unit, so we instead are running the servo off of a 5V supply and are using another variable supply as an analogue for the battery. While not ideal, this allows us to showcase all the functionality the code has to offer.